Hello,
I set up the transceiver in the nib and also tried manually in the ybts.conf , when I probe bladerf or info everything seems properly working (FPGA loaded and all).
bladeRF> info
Serial #: 2c77309e4cf55388978bd44e5ac352b9
VCTCXO DAC calibration: 0x9650
FPGA size: 115 KLE
FPGA loaded: yes
USB bus: 2
USB address: 2
USB speed: SuperSpeed
Backend: libusb
Instance: 0
Logs :
2015-06-03_23:15:02.808998 <ybts:NOTE> State changed WaitHandshake -> Running
2015-06-03_23:15:02.809022 <ybts-signalling:INFO> Sending [0x253d330]
-----
Primitive: Handshake
Info: 0
-----
2015-06-03_23:15:02.829508 <javascript:INFO> Parsed 'nib' script: /usr/local/share/yate/scripts/nib.js
2015-06-03_23:15:02.831382 <nib:CONF> Please configure country code. See subscribers.conf or use the NIB web interface
2015-06-03_23:15:02.832212 <NOTE> Failed to open config file '/usr/local/etc/yate/tmsidata.conf', using defaults (2: No such file or directory)
2015-06-03_23:15:02.832411 <nib:INFO> Finished reading saved registered subscribers. Found 0 registered_subscribers.
2015-06-03_23:15:02.832774 <nib:INFO> Checked that only NIB is enabled.
2015-06-03_23:15:02.832831 <ALL> Rescanning handler list for 'engine.start' [0x7ffcaa0fd020] at priority 100
Yate engine is initialized and starting up on lpt
2015-06-03_23:15:02.832922 <INFO> Creating first message dispatching thread
2015-06-03_23:15:03.725090 <cpuload:NOTE> Updating CPU core number from 1 to 4
2015-06-03_23:15:03.809995 <mbts:MILD> TRXManager.cpp:283:sendCommandPacket: TRX link timeout on attempt 1
2015-06-03_23:15:04.810642 <mbts:MILD> TRXManager.cpp:283:sendCommandPacket: TRX link timeout on attempt 2
2015-06-03_23:15:05.811791 <mbts:MILD> TRXManager.cpp:283:sendCommandPacket: TRX link timeout on attempt 3
2015-06-03_23:15:06.812588 <mbts:MILD> TRXManager.cpp:283:sendCommandPacket: TRX link timeout on attempt 4
ALERT 140467719026496 23:15:07.8 TRXManager.cpp:432:powerOff: POWEROFF failed with status -12015-06-03_23:15:07.813478 <mbts:MILD> TRXManager.c$
2015-06-03_23:15:07.813518 <mbts:NOTE> TRXManager.cpp:293:sendCommandPacket: lost control link to transceiver
2015-06-03_23:15:07.813530 <mbts:WARN> TRXManager.cpp:432:powerOff: POWEROFF failed with status -1
2015-06-03_23:15:07.890610 <mbts:NOTE> OpenBTS.cpp:145:startTransceiver: starting transceiver ./transceiver-bladerf w/ 1 ARFCNs and Args:
EMERG 140467718141696 23:15:07.8 OpenBTS.cpp:151:startTransceiver: cannot find ./transceiver-bladerf
2015-06-03_23:15:07.890780 <mbts:GOON> OpenBTS.cpp:151:startTransceiver: cannot find ./transceiver-bladerf
EMERG 140467718141696 23:15:07.8 OpenBTS.cpp:159:startTransceiver: Transceiver quit with status 256. Exiting.
2015-06-03_23:15:07.890868 <mbts:GOON> OpenBTS.cpp:159:startTransceiver: Transceiver quit with status 256. Exiting.
2015-06-03_23:15:11.013331 <ybts:NOTE> Peer pid 24186 vanished
2015-06-03_23:15:11.013373 <ybts:ALL> Restart scheduled in 1ms [0x7ff8cf6b6580]
2015-06-03_23:15:11.013383 <ybts:ALL> Scheduled stop in 0ms
2015-06-03_23:15:12.012003 <ybts:NOTE> 'shutdown' command failed
I dont know what I'm doing wrong.